KTX의 모터블록 성능부족 개선 실행

Action to improve 'lack of performance' of KTX motor bloc

  • 강기석 (한국철도공사 수도권철도차량관리단 고속차량전기팀) ;
  • 김진규 (한국철도공사 차량기술단 고속차량팀)
  • 발행 : 2009.05.21

초록

Since opening of the high speed railroad in Korea, service result of the last 5 years is commandable. About 236million passengers had taken KTX until February 2009, and number of trains in service per day during week-end increased from 128 to 181, meaning that it's grown about 40%. And MKBSF, one of indicators of the high speed railroad's reliability, registered 680,469Km at the end of the year 2008, witch is 6 times more than 121,000Km, contract base when KTX was introduced. With increasing number of trains in service, not only passengers use the high speed railroad more frequently, but also we assure its reliability through maintenance based on reliability. And actually we gather information concerning all kind of defects occurred during train circulation and then, analyse them, and eradicate their causes in order to improve the high speed railroad's reliability. This paper describes a verification test process to analyse causes of defective function about train's traction.

키워드