The Effect of the ZLR and Tied Sleeper to Reduce the Track Irregularity in the Bridge Expansion Joint Zone

교량신축부에서의 궤도틀림 저감을 위한 활동체결구 및 침목결속 효과

  • 강태구 (코레일, 오송고속철도시설사무소) ;
  • 민경주 ((주)철도안전연구소) ;
  • 임남형 (충남대학교, 토목공학과)
  • Published : 2011.10.20

Abstract

In recent time, the cause analysis and the reduction of the track irregularity have become the most important issue in the ballasted track on the high-speed railway bridge. This is because that the frequency of the maintenance work at the bridge expansion joint zone is on the rise. The track irregularity on the railway bridge starts at the end of the bridge-deck and spreads along the bridge. Due to the dynamic vibration and the thermal expansion of the bridge, the compaction of the ballast gravel on the bridge expansion joint zone become loose and then the progress of the track irregularity result from the train-induced dynamic impact is accelerating further. Among the several options for reducing the track irregularity on the bridge expansion joint zone, the application and efficiency of the zero longitudinal restraint(ZLR) and tied sleeper are investigated in this paper. Field test construction has been conducted, then the progress of the track irregularity and the frequency of the maintenance work are analyzed before and after the filed test construction. Of the two methods, it is shown that the installation of the ZLR seems to be better than the tied sleeper.

Keywords