A Study on the improvement of treatment efficiency in a conventional sewage treatment plant

기존 하수처리장에서의 처리 효율개선에 관한 연구

  • Published : 2000.09.01

Abstract

In this study, sewage were treated with operating Two-step Aeration System and conventional activated sludge process together in a condition. At the same HRT 8hr of Two-step Aeration System and Activated Sludge Process, BOD treatment efficiency of 1st sedimentation basin effluent 36.9% by Two-step Aeration system was 12.3% higher than 24.65 by Activated Sludge Process and the COD treatment efficiency 39.8% by two-step Aeration System was 11.6.3% higher than 28.2% by Activated Sludge Process. BOD and COD treatment efficiencies of 2nd sedimentation basin effluent were 88.1% and 85.6% Two-step Aeration System and were 83.8% and 82.3% Activated Sludge Process. In the first treatment, as BOD was relatively removed a lot, F/M ratio 0.17, $0.21{\cdot}BOD/kg{\cdot}MLSS.d$ was maintained by Activated Sludge Process. Therefore it was proved that organic matter treatment efficiency by Two-step Aeration System os Higher than by Activated Sludge Process in a aeration time 8hr. $NH_4^{+}-N$ treatment efficiencies were 55.5% by Two-step Aeration System and 39.75 by Activated sludge Process. $NO_3^{-}-N$ concentration in 2nd. sedimentation basin effluent were 3.33% by Two-step Aeration System and 2.36% by Activated Sludge Process. From this result, Two-step Aeration System was proved more advantageous treatment process for nitrification than Activated Sludge Process. The fluctuation range of BOD, COD and SS concentration in 2nd sedimentation basin effluent $16~33mg/{\ell}$, $15~23mg/{\ell}$ and $14~22mg/{\ell}$ by Two-step Aeration System was smaller than $16~57mg/{\ell}$, $15~25mg/{\ell}$ by Activated sludge Process. Overall the fluctuation range in 2nd sediment basin effluent by was smaller than by Activated Sludge Process. As a result, it is possible for this Two-step Aeration with no facility investment and a little of operation condition change in a conventional sewage treatment plant to get stability and nitrification of treatment water quality.

Keywords

References

  1. 환경백서 N, N.
  2. 2000 환경산업총람 N, N.
  3. 동아대학교 환경문제 연구소 연구보고 v.13 no.1 2단폭기방식에 의한 제지폐수처리 효과분석 지기원
  4. 2단폭기에 의한 피혁폐수 처리연구 정익상
  5. 2단폭기방법에 의한 염색폐수처리 안종수
  6. durch Einsatz Mohrstufiger Biologischer Verfahren seminar 2 Leistangssteigssteigerung und Energiekostensenkung Bohnke
  7. Gewassensehututz und Gesetzzebung und Ihre Aus-winkungen aufdie Auslegung komm Nasler klaranlagen KA 281 Bohnke, B.
  8. Das A-B Verfahren Zur Biologischen ABwasserringung Bohnke, B.
  9. Erfahrungen ans aweistufigen Wersachsanlangen und Folgerungen fuer die Verfahrenstechnik korrespondenc Abwasser v.27 no.3 Bohnke, B.
  10. 하수도·폐수처리 핸드북 Imhoff