DOI QR코드

DOI QR Code

Effect of Tip Clearance on the Performance of a Turbopump Inducer

끝틈새가 터보펌프 인듀서의 성능에 미치는 영향

  • 홍순삼 (한국항공우주연구원 터보펌프그룹) ;
  • 김진선 (한국항공우주연구원 터보펌프그룹) ;
  • 최창호 (한국항공우주연구원 터보펌프그룹) ;
  • 김진한 (한국항공우주연구원 터보펌프그룹)
  • Published : 2006.02.01

Abstract

Experiments are carried out to investigate the effect of radial tip clearance on a turbopump inducer, which has two blades with inlet tip blade angle of 7.8 degree and tip solidity of 2.7. Hydraulic and cavitation tests are performed for three cases of tip clearance ratio, that is, 0.026, 0.053, and 0.079. With increase in the tip clearance, inducer head and pressure on the inducer tip decrease. Attached cavitation and cavitation surge are observed in the cavitation tests. In the attached cavitation one cell rotates at the same rotational speed as that of the inducer. Cavitation performance deteriorates with increase in the tip clearance. The level of casing vibration increases in the cavitation condition and the level is very high when the attached cavitation appears.

Keywords

References

  1. Lee, S., Jung, K., Kim, J., Kang, S., 2002, 'Cavitation Mode Analysis of Pump Inducer,' KSME International Journal, Vol. 16, pp. 1497-1510
  2. Tsuiimoto, Y., Yoshida, Y., Maekawa, Y., Watanabe, S., Hashimoto, T., 1997, 'Observations of Oscillating Cavitation of an Inducer,' ASME Journal of Fluids Engineering, Vol. 119, pp. 775-781 https://doi.org/10.1115/1.2819497
  3. Furukawa, A., Ishizaka, K., Watanabe, S., 2002, 'Experimental Study of Cavitation Induced Oscillation in Two Bladed Inducers,' 4th International Conference on Launcher Technology, Space Launcher Liquid Propulsion, Liege, Belgium, 3-6 December
  4. 홍순삼, 김진선, 최창호, 김진한, 2005, '터보펌프 인듀서의 비정상 캐비테이션에 관한 실험적 연구' ,유체기계저널, 제8권, 제1호, pp. 23-29 https://doi.org/10.5293/KFMA.2005.8.1.023
  5. 홍순삼, 최창호, 김진한, 2004, '현절비가 터보펌프 인듀서의 성능에 미치는 영향', 대한기계학회논문집 B권, 제28권, 제4호, pp. 382-388 https://doi.org/10.3795/KSME-B.2004.28.4.382
  6. 김진선, 홍순삼, 최창호, 김진한, 조광래, 2003, '날개각이 터보펌프 인듀서의 성능에 미치는 영향', 한국항공우주학회 추계학술대회 논문집, pp. 1059-1062
  7. 홍순삼, 구현철, 차봉준, 김진한, 2003, '터보펌프 인듀서의 출구 유동 및 성능 특성', 유체기계저널, 제6권, 제4호, pp. 38-44 https://doi.org/10.5293/KFMA.2003.6.4.038
  8. Jakobsen, J. K., 1971, 'Liquid Rocket Engine Turbopump Inducers,' NASA SP-8052

Cited by

  1. Effect of the number of blades on the performance and cavitation instabilities of a turbopump inducer with an identical solidity vol.29, pp.12, 2015, https://doi.org/10.1007/s12206-015-1126-6