• Title/Summary/Keyword: High-Speed Unwinding

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Experimental Verification of Unwinding Behavior of Fiber-Optic Cable and Prediction of High-Speed Unwinding (광 케이블 풀림 거동의 실험적 검증 및 고속 풀림 거동 예측)

  • Kim, Kun Woo;Lee, Jae Wook;Kim, Hyung Ryul;Yoo, Wan Suk
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.38 no.3
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    • pp.243-250
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    • 2014
  • Fiber-optic cables towed by underwater vehicles have an important role in enhancing the mission capability of a mother ship. In general, fiber optic cables are unwound in water for securing unwinding stability and preventing unwinding-related problems. Therefore, in this study, the numerically simulated result is verified against the experimental result in water, and the cable-unwinding motion is predicted based on the increase in unwinding velocity. The experimental apparatus is composed of a water tank and a winder, and a high-speed camera is used for photographing the cable-unwinding motion. The numerical result defined in the Cartesian coordinate system is solved using a transient-state unwinding equation of motion. The numerical result agrees well with the experimental result, and it can predict cable-unwinding behaviors in according to an increase in the unwinding velocity.

Domestic Development of Vibrational Film Forming Machine and Die and Mold in the High Speed Production(I) - Single production forming machine - (고속 생산형 필름 진동판 성형기 및 금형 국산화 개발(I) - 단수 생산 진동판 성형기 -)

  • Kim, Jung-Hyun
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.11 no.6
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    • pp.9-15
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    • 2012
  • Vibrational film has been more employed in ear-phones or small type of speakers along with a wide use of portable multi-media equipments such as MP3 and MP4. However, the current hand work production process of diaphragms is inefficient. In this study, a die-and-mold and a single production forming machine are developed, and they result in a multi-production forming machine. The multi-production forming machine consists primarily of a film feeding unit and an unwinding unit. A vacuum suction device provides the film feeding unit, while the unwinding unit is obtained using an appropriate damper. The advantage of the developed single production forming machine is shown according to a proper voice test.

Analysis of tension properties at roll changing process of a high speed printing machine (고속인쇄기 롤 교체과정의 장력특성 해석)

  • Lee B.J.;Kim S.H.;Kang C.G.
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2006.05a
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    • pp.281-282
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    • 2006
  • Tension control performance is very important in high-speed printing machine. One of the major factors that effect to tension control performance is the process of roll changing. Even if the turret arm moves during roll changing process and the span length of the unwinding system varies, it is customary to neglect it in motion and tension control and to consider it as a disturbance. In this paper, its effect is modeled nonlinearly and compared with linear model, and an effect of an infeeder dancer is analyzed under the condition with no unwinder dancer. We verify the performance of the proposed method via simulation in the high-speed printing machine.

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Domestic Development of Vibrational Film Forming Machine and Die in the High Speed Production(II) - Multi-production forming machine - (고속 생산형 필름 진동판 성형기 및 금형 국산화 개발(II) - 다량 생산 진동판 성형기 -)

  • Kim, Jungl-Hyun
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.13 no.1
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    • pp.52-58
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    • 2014
  • This study consists of two parts. The first discusses the development of a single production forming machine which was reported in earlier papers. The second outlines the development of a multi-production forming machine, which consists primarily of a film feeding unit, an unwinding unit, and a heating block unit. The heating block unit of the multi-production forming machine has 30 members per die. An analysis of the stress deformation and temperature deviation of this machine is carried out using ANSYS Workbench and CFX-11 under the design conditions. According to this analysis, the maximum deflection in the Z-direction is $0.05104{\mu}m$ and the maximum temperature deviation is $0.7^{\circ}C$ when the temperature of the heating block unit is $175^{\circ}C$. It was also found that these values are structurally safe. The advantage of the developed multi-production forming machine is demonstrated to be in its offering of a proper voice test.

Development of Defects Detecting System for Corrugated Board, Mill Application, and Changes of Production Defects Ratio (골판지 불량 검색 시스템 개발, 현장적용과 생산 불량률 변화)

  • Jeong, Jin-Mo;Min, Kyung-Eun;Kim, Mun-Sung;Park, Jong-Moon
    • Journal of Korea Technical Association of The Pulp and Paper Industry
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    • v.40 no.2
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    • pp.37-42
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    • 2008
  • Defects of corrugated board were limiting factors to the corrugated industry's growth. On-line detecting systems of defects are beneficial to increase profits of the corrugated board companies by reducing base paper consumption, increasing process reliability, and increasing productivity. By replacing naked eye inspection of defects to a defects detecting system, continuous inspection without fatigue may guarantee final products quality. The system was developed, which was consisted of line scan CCD camera, lens, illuminating parts, high speed image processor, software, various input parts, and output parts. First installation location of the system was at before fluting process after base paper unwinding, and surface of liner board was inspected by the system. Second installation location was after fluting process and combining process for liner board. Production loss includes ragged appearance of edge, irregular flute shape, wrong combination of flute, score cracking, defects in base paper, and flute cracking. The production loss was analyzed before and after the system installation at a commercial domestic mill. The production loss ratio was defined as a production loss weight per total production weight. The production loss ratio before the installation was decreased a lot from 1.28%(during 3 months before installation) to 0.76%(during 12 months after the first installation) and to 0.25%(during 6 months after the second installation).