• Title/Summary/Keyword: anti-washout admixture

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Effect of Anti-washout Admixture Implementation on Backfill Aggregates on Underwater Structures (수중 구조물 골재 속채움 시 수중 불분리성 혼화제의 적용 효과)

  • Kim, Ukgie;Choi, Changho;Park, Bonggeun;Li, Zhuang;Cho, Samdeok
    • Journal of the Korean GEO-environmental Society
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    • v.15 no.9
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    • pp.59-67
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    • 2014
  • With increasing underwater structure construction, there is high interest in offshore foundation and underwater grout and various study has been done in this area. For grout materials constructed underwater, it may be washed away by water or easily disturbed and material separation phenomenon during curing period always happens. As a result, it is difficult to ensure construction quality and this has a significant influence on the design strength of structure. In this study, to understand application effects of anti-washout admixture for the preplaced construction method, where grout is injected in monopile after filled with aggregates, laboratory tests on bleeding and compressive strength of anti-washout admixture were performed under various test conditions varying size of aggregate, water and cement ratio and admixture, and test results were compared and evaluated.

Study on Anti-Washout Properties and Shear-Thickening Behaviors of Surfactant Added Cement Grouts (계면활성제 혼화제를 첨가한 시멘트 그라우트의 수중 불분리 특성 발현과 점도 증가 효과 연구)

  • Jang, In-Kyu;Seo, Seung-Ree;Park, Seung-Kyu
    • Applied Chemistry for Engineering
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    • v.23 no.5
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    • pp.480-484
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    • 2012
  • Concrete, the mixture of cement, sand, gravel and water, is a suspension substance extensively used to construct building materials. When a concrete mortar is applied to the underwater construction, the rheology of concrete is of great importance to its flow performance, placement, anti-washout and consolidation. In this research, the anti-washout and rheological properties of concrete have been investigated with concrete admixtures prepared by adding anionic surfactants, cationic surfactants, and polymeric thickeners. The concrete mortar formulated by pseudo-polymeric systems with the electrostatic association of anionic and cationic surfactants, showed high viscosities and suitable anti-washout properties, but poor pumpabilities. The addition of poly methyl vinyl ether to the mixed surfactant system exhibits synergistic effects by improving the concrete mortar properties of the concrete mortar such as fluidity, visco-elastic property, self-leveling, and anti-washout.

An Experimental Study of Chloride Acceleration on the Seawater Resistance of Fly Ash Antiwashout Underwater Concrete (플라이애쉬 수중불분리성 콘크리트의 내해수성에 관한 염화물 촉진 시험)

  • Kwon, Jung-Hyun;Kim, Bong-Ik
    • Journal of Ocean Engineering and Technology
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    • v.19 no.6 s.67
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    • pp.29-34
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    • 2005
  • This paper describes the effect of fly ash replacement on seawater resistance of anti-washout underwater concrete, which was replaced cement by fly ash from $0\%$ to $50\%$. The experimental work was performed to find out the variations of length and weight of specimens, using a chloride acceleration test in $40\^{\circ}$C The results shaw that the admixture using fly ash on an anti-washcout underwater concrete in the sea environment makes it more durable for the attacks of chloride by seawater. Also, the length of specimens of anti-washout underwater concrete, at age 180 days, increased substantially, compared with normal concrete; however, the mixture in which cement was replaced $50\%$ of fly ash shows $93\%$ reduction of the expansion, compared with the normal anti "washout underwater concrete specimen.

Evaluation of Mixing Conditions for the Production of Optimized High Flowing Concrete

  • Kim, Sang-Chel
    • KCI Concrete Journal
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    • v.11 no.3
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    • pp.79-88
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    • 1999
  • Most difficulties of inducing high fluidity on the concrete mixing design with a strength range of 210 to 240kg/$\textrm{cm}^2$ result from the segregation of aggregates due to the shortage of cementitious binders. To solve the problem, this study concentrated on finding the optimized amount of binder material which does not affect the concrete strength and is also economical. Also there were studies on the use of intermediate sized aggregates to avoid the gap-grading between coarse and fine aggregates so that the material segregation in high flowing concrete was and minimalized the fluidity and penetration capacity of the reinforcing bars was enhanced. Throughout the parametric study with respect to water/binder ratio. superplasticizer. replaceable mineral admixture, the size of coarse aggregate and mixing methods, the effect of each constituent on the characteristics of high flowing concrete could be observed. As a result or partially using stone powder or an intermediate class of aggregate (max. diameter 13mm) . it was fund that the fluidity of concrete significantly increased without material segregation and any change of compressive strengths. It was also proved in this study that proper mixing time and speed are significant factors influence the performence of high flowing concrete.

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Quality Evaluation and Mix Proportion of Antiwashout Underwater Concrete with Mineral Admixture (광물질 혼화재료를 사용한 수중불분리성 콘크리트의 배합 및 품질평가 방안 검토)

  • Park, Yong Kyu;Kim, Hyun Woo;Yoon, Ki Woon
    • Journal of the Korea Concrete Institute
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    • v.26 no.6
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    • pp.679-686
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    • 2014
  • In this research, the mix proportion of the antiwashout underwater concrete with the mineral admixture was evaluated. It can reduce the amount used of the antiwashout admixture (hereinafter referred to as "AWA") and satisfy the properties of concrete. In addition, the review for the difference of the test and practical affairs were conducted. Optimized unit quantity of water of antiwashout underwater concrete and the amount used of AWA was revealed by $190kg/m^3$, 0.9%/W, respectively. In particularly, the mix design is reduced by 5% than the W/B of target strength even though the W and AWA reduced. Therefore, it will have the economical feasibility and qualities including the material separation, resistance characteristic and compressive strength, and etc. The stable value was shown in 1 point of minute passed in the measurement of the turbidity amounts using the turbidimeter after the checker insertion. However, it needs to be reviewed for the interrelationship between turbidity measuring machine and KCI-AD102 standard method. There were no significant differences of compressive strength of specimens in the water depending on the production methods.

A Case Study on Caisson Foundation Grouting in Geo-Ga Bridge (거가대교 케이슨기초 그라우트 충전 사례연구)

  • Bae, Kyung-Tae;Cha, Kyung-Seob;Kim, Young-Jin;Park, Chung-Whan;Jeong, Gyeong-Hwan
    • Proceedings of the Korean Geotechical Society Conference
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    • 2010.03a
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    • pp.1046-1050
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    • 2010
  • During construction of a sea-crossing bridge grouting was used to fill densely the space between the bottom of caisson and the ground. This grout mixture was mixed with an anti-washout admixture after locating accurately the pre-cast caisson on three concrete landing pads. This method differs significantly from the costly conventional method, for bridge foundations offshore, where concrete is placed in situ after excavating inside of a temporary concrete coffering wall. To verify the grouting method in advance, the full-scale field tests were performed twice on land. After identifying the fluidity of the grout material to be filled, finding some possible problems with the main construction and revising the original design, the main construction has been continuing successfully with 20 caissons completed to date. The purpose of this paper is to introduce for the first time in Korea the grouting method including the automatic and the manual monitoring system based on the main construction of the caisson foundation.

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Application of Grouting of the Sea-Crossing Bridge Foundation in Busan-Geoje Fixed Link (부산~거제간 연결도로 해상교량기초 그라우팅 시공사례 연구)

  • Park, Chung-Whan;Jeong, Sang-Kyoon;Jeong, Gyeong-Hwan;Shin, Min-Sik;Park, Chan-Woo;Kwon, Jin-Wook
    • Proceedings of the Korean Geotechical Society Conference
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    • 2007.09a
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    • pp.665-678
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    • 2007
  • It was applied the grouting method to fill densely the space between the bottom of the caisson and the ground with the grout mixture mixed with anti-washout admixture after locating accurately the precast caisson on three concrete landing pads but it is far different from a costly conventional method, which place concrete to build the foundation of reinforcement concrete on the spot after excavating inside of the temporary coffering wall for the bridge foundation in the sea. To verify the grouting method in advance, the full-scale trial test was performed twice on the land. After confirming the fluidity of material for the injection and some possible problems during construction and then enhancing the original design, the main process is ongoing and it has been finished 12 spots until now. The purpose of this study is to introduces for the first time in Korea the grouting method including the automatic and the manual monitoring process applied to, based on the main process of the caisson foundation finished already in the site. In a similar construction it is sincerely expected to be referred to in the future.

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