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Performance Test of A Reverse-Annular Type Combustor (TS2) for APU

보조동력장치용 환형 역류형 연소기 (TS2) 성능 시험

  • Published : 2002.06.01

Abstract

Development of a small gas-turbine combustor for 100㎾ class APU(Auxiliary Power Unit) has been performed. This combustor is a reverse-annular type and has a tangential swiller in the liner head to improve the fuel/air mixing and flame stability. Three main and three pilot fuel injectors of the simplex pressure-swirl type are used. The performance target at the design condition includes a turbine inlet temperature of l170k, a combustion efficiency of 99%, a pattern factor of 30%, and an engine durability of 3000 hours. Under developing the combustor, we conducted the performance test of our first prototype(TS1) with some variants. As a result of the test, the performance targets of the combustor are satisfied except that the pattern factor is about 4% higher than the target value. Therefore, the second prototype(TS2) was redesigned and the performance test was conducted with the critical focus on the pattern factor and the exit mean temperature. We adopted TS2 four variants to check the improvement of the pattern factor. As a result, the pattern factors of several variants were satisfied with the performance target. Finally, the TS2A variant was chosen as a final combustor fur our APU model.

Keywords

References

  1. Ahn, Kook-Young, Kim, Han-Seok, Antonovksy, V. I., 2001, 'Model and Field Testing of a Heavy-Duty Gas Turbine Compbustor,' KSME International Journal, Vol. 15, No. 9, pp. 1319-1327 https://doi.org/10.1007/BF03185673
  2. Lefebvre, A. H., 1983, Gas Turbine Combustion, McGraw-Hill
  3. Odger, J. et al., 1980, The Design and Development of Gas Turbine Combustors, Nothern Research and Engineering Corp
  4. NREC Report No.1344-1,1980, The Design And Development of Gas Turbine Combustors : Volume I Component Theory and Practice, NREC
  5. 고영성, 한영민, 양수석, 이대성, 김명환, 최성만, 2000, '보조동력장치용 환형 역류형 연소기시험,' 한국항공우주공학회 춘계학술대회, pp. 508-512
  6. 고영성, 한영민, 양수석, 이대성, 윤상식, 최성만, 2001, '보조동력장치용 환형 역류형 연소기(TS1) 성능 시험,' 한국항공우주공학회 춘계학술대회, pp. 196-200
  7. 고영성, 한영민, 양수석, 이대성, 2000, '보조동력장치용 환형 역류형 연소기 성능 시험(I),' 한국항공우주공학회 제28권 8호, pp. 109-114
  8. 이대성, 차봉준, 한영민, 윤민수, 김춘택, 고영성, 2000, '한국항공우주연구소 가스터빈 엔진 요소부품 및 시스템 성능시험기,' 한국항공우주학회지 제28권 1호, pp. 166-176
  9. 이동훈, 최성만, 한영민, 고영성, 2001, '환형 역류형 APU 연소기 성능특성 연구,' 제22회 KOSCO SYMPOSIUM 논문집, pp. 67-74
  10. 제 22회 KOSCO SYMPOSIUM 논문집 환형 역류형 APU 연소기 성능특성 연구 이동훈;최성만;한영민;고영성